The Shop

The Shop
My name is Jake Rendell. This blog is a description of the various skills and information that I have learned and will learn while studying at Minnesota State Southeast Technical, in the Band Instrument Repair Program. Before coming to study in the BIR Program, I graduated cum laude from Laurentian University with a B.A. Music - Vocal in 2010, and First Class Standing with a B.Ed. I/S Music from Lakehead University in 2011. This final certification from MSC-ST will finish in May of 2012. I will try to update this blog on a weekly basis.

Week 20 - January 23rd - 27th

What a busy week here in the Brass Lab. The work has been picking up as we finish up casing/piston repair and get into full swing with the French Horn.

To start the week off, I aligned an out-of-round piston on a cornet. This piston had some major issues, including a large bend, and some small dents all over the surface. To begin, I found where the fulcrum of the large dent was and, using the bottom of the casing as a pivot point, hit the piston with a mallet to bring down the dent. This was somewhat successful, but do to the other issues involved, not very. Next I used a sized sleeve as a swedging die to remove some of the out-of-round damage from the piston. This was very successful. Before reinstalling the piston, there were a few dents that hadn't been totally removed from the casing, so using a slotted casing mandrel I burnished them to smooth. The piston will never feel like new again, but it is definitely playable.

 

 Moving on to the project French Horn, someone put a pretty gnarly flat spot into this tuning slide. I began by removing the little bit of excess solder from the inside of the tube so that I could reach the dent. Using a Ferree's driver, I pushed dent balls through the crook to expand it back to round. Unfortunately, this crook is ridiculously strong. In order to get more pressure, I switched to the Roth tool. After the dents were brought out, there was a very sharp ridge left on the inside rim. Using a Delrin mallet and a draw plate, I managed to smooth the ridge a little. There is still evidence that there was a dent on that crook, but it has come a long way.


 

On to bell dents. The French Horn has a large bell. As a result, the brass gets very thin towards the bell. This makes it very easy to dent, even on a thick horn like this one. So using a bell iron and a roller, I went around the entire bell flare looking for small dents that needed to be removed. Further up the bell into the stem there were two more severe dents that had to be removed. Both were sharp and both were deep. To remove them, I used a series of dent balls on a french horn mandrel to raise the dent to surface and tap on it. After repeating this process several times, the dents were as good as gone.



Continuing down the bell stem towards the ferrule, I encountered a smashed in finger hood. This is not an uncommon dent. To remove it, we must first remove the finger hook. While already set up at the soldering bench, I soldered a dent puller into the crease of the dent. With a hefty weight on its shaft, this puller can be used to put quite a bit of force on the dent, pulling it up enough to get a dent ball in. Once it was pulled up, I used a series of dent balls strung down a cable to knock the dent out. The dent is now mostly out and will be burnished next week.



Towards the end of the week, we looked at restringing French Horn rotors. This process was actually more complicated than I expected. We began by removing all of the levers from the horn and aligning them. After reinstalling them, we string the rotor using the "Three Under" method. It is very difficult to explain, but it strings the horn in a way that allows you to adjust the height of the key with one screw, and doesn't leave any slop. The three levers were strung and leveled to each other perfectly.
 

 Like on trumpets, the tubes on a horn get bent and knocked out of alignment. One issue that I was having was the mouthpipe receiver end was bent in at the brace. To fix this, I used a piccolo mandrel inside the mouthpipe and simply bent it back. Nothing fancy, but it's in line now.


While this is not my work, I felt it was worth showing. This video is of Doug bending a cornet mouthpipe to replace on a project horn. This pipe is filled with a tar-like substance called pitch, to stop it from crimping when bending. Take note of his hand position, his speed and the position of the pipe in the vice. It is important that the tube does not move on the jig, and that the speed is constant to avoid crimping. This was his first attempt. It did not bend as far as he would have liked, but the bend was smooth. After some minor adjusting, he fit it to the cornet well. Enjoy.


Finally, I would like to note that our program was featured on a television program a couple of weeks ago. The camera crews came in before the Christmas Break and took some snazzy shots. The segment was very well done and quite informative. You can find it at http://www.kstp.com/article/12303/?vid=3168482&v=1   Enjoy.

Week 19 - January 16th - 20th

 Good afternoon followers. This week has been an exciting one here in the brass lab as we start to deal with pistons and casings. Issues with the pistons and casings can be very troublesome. With the tolerances of today's horns, the smallest dent can seriously inhibit the horn's ability to function. Valves easily get stuck and the horn no longer plays. This week we learn how to rectify some of the issues that cause this.

We start off this week with damaged bottom cap threads. You may recall that I had this issue on my project trumpet last semester, and I went about fixing this the same way. Using dent balls, I worked the bottom of the casing back to round. I then used the bottom cap, and the Ferree's thread burnisher to rework the threads that were damaged in the bend. After a little bit of chasing and working, the bottom cap threaded on like new.
Last Semester
This Semester

 The next issue to deal with was dented casings. A small ping dent like this one may not look like much, but it was enough that that piston wouldn't move. To take this out, I first cleaned the casing to a nice shine with a brass brush and Scotch Brite. Using a ground casing mandrel, I hammered the dent down with a series of mallets and hammers ranging from leather-faced rawhide to stainless steel. After a little bit of working and a bit more cleaning, the dent was down and the piston was free.

We started getting into French Horns this week as well. My project horn is an Oxford double horn. It's a heavy junker that's missing a few parts and has more than a few dents. To get her prepped for dent work, I stripped her down and started cleaning. Like the trumpets, I began by pre-cleaning all of the slides, inside and out. I also disassembled the rotors and cleaned them. It all took a bath in simple-green solution for the gunk, and phosphoric acid for the corrosion. I learned that rotors can be particularly corroded in older horns, so after 4 baths in phosphoric acid I stepped it up to muriatic acid, which is diluted hydrochloric. A few rinses with that cleaned it right up. All of the bare brass got stabilized and she is now ready for some dent work.


Week 18 - January 9th - 13th

Welcome back to Red Wing MN! Hope you all had a fantastic holiday season because we're back in the swing of things here. This week in the brass lab we began with some review on dent work and soldering, along with some new tools and lathe work.

First off this week, we began my modifying a standard solder clip to create a draw knob installer. On many of the smaller crooks, the draw knobs do not have flanges on the bottom to hold on to while soldering. This clip allows us to hold the knob firmly in place while soldering. We began by shaping a steel bit into a shallow cup with a beveled back. We then increased the tension on the clip to hold the cup properly. Finally, we silver soldered the cup in place and pickled it. Simple and effective.

Throughout the week we've been working on a cornet bell in preparation for job interview bench tests. So far this has included soldering a supporting brace on the tail, soldering a patch onto the stem, removing dents from the bow, stem and flare and removing a bell fold.


We began working on aligning fast slides on intermediate and professional trumpets. This involved removing dents and lapping the tubes to make sure they fit. Then by flexing the first and third slide tubes, we aligned them to move as quickly as possible.
Finally this week, we worked on a lathe project. We turned these plates into a rotor bearing plate burnisher. These blanks were made by the machining class in Winona. We then faced them and drilled a hole in the center. We then drilled a counter bore in the center and tapped the hole. This simple tool will allow us to burnish french horn rotor bearing plates to friction fit after they have worn.